DragonFly kernel List (threaded) for 2008-12
[
Date Prev][
Date Next]
[
Thread Prev][
Thread Next]
[
Date Index][
Thread Index]
Struggling with VirtualBox
Hi,
I'm still trying to get DragonFly reliably working on VirtualBox (just because Qemu on my Ubuntu doesn't like to run with the
accelerator kqemu).
So I modified DELAY to break out if delta <= 0. Together with acpi_load=YES I can boot, but:
- When I boot for the first time ("turn power on"), pressing a key in the boot menu (the "1. Boot DragonFly [default]" ... "7. Reboot" menu)
will freeze the system.
- Or if I let the countdown timer pass, it will just execute for a very show while to then begin to spin in DELAY with delta=0
and ticks_left=2 [1].
- If I now reset the system, the boot menu works (pressing a key doesn't freeze the system anymore). And I can also boot into DragonFly.
The patch I am using is appended. I am thankful for any hints or further suggestions what the reason for this strange behaviour could be!
Also note that the clock calibration returns a difference of more than 1%.
Matt, you suggested a while ago, to use the APIC timer and get completely rid of the 8254 timer. If you could give me a starting point
I'd like to try that out. At least I can now boot and successuflly compile a kernel in VirtualBox, which is a big help in testing things
out.
Regards,
Michael
[1]: Notice that I only break the loop while in startrtclock(). At the end of this function, I reset cold_delay_timer to 0.
diff --git a/sys/platform/pc32/isa/clock.c b/sys/platform/pc32/isa/clock.c
index f02333d..170a240 100644
--- a/sys/platform/pc32/isa/clock.c
+++ b/sys/platform/pc32/isa/clock.c
@@ -152,6 +152,8 @@ static struct cputimer i8254_cputimer = {
0, 0, 0
};
+static int cold_delay_timer = 1;
+
/*
* timer0 clock interrupt. Timer0 is in one-shot mode and has stopped
* counting as of this interrupt. We use timer1 in free-running mode (not
@@ -415,8 +417,18 @@ DODELAY(int n, int doswitch)
#endif
delta = tick - prev_tick;
prev_tick = tick;
- if (delta < 0)
+
+ if (delta <= 0) {
+ /* break delay loop during early boot as
+ the timer might not be correctly working */
+ if (cold_delay_timer) {
+ break;
+ } else {
+ kprintf("delta: %d, ticks_left: %d\n",
+ delta, ticks_left);
+ }
delta = 0;
+ }
ticks_left -= delta;
if (doswitch && ticks_left > 0)
lwkt_switch();
@@ -600,6 +612,7 @@ fail:
static void
i8254_restore(void)
{
+ kprintf("i8254_restore\n");
timer0_state = ACQUIRED;
clock_lock();
@@ -794,6 +807,11 @@ startrtclock(void)
#endif
}
+ /* Timer should now work correctly! */
+ cold_delay_timer = 0;
+ //if (bootverbose)
+ kprintf("cold_delay_timer -> 0\n");
+
EVENTHANDLER_REGISTER(shutdown_post_sync, resettodr_on_shutdown, NULL, SHUTDOWN_PRI_LAST);
#if !defined(SMP)
[
Date Prev][
Date Next]
[
Thread Prev][
Thread Next]
[
Date Index][
Thread Index]